Took the carbs to bits again and replaced the following based on the Haynes and Steve's list:
- Needle jets
Main jets
Main jet washers
Needles
O-rings including aux carb
New throttle springs
I took off the floats and cleaned the float needle
Cleaned the pilot jet and mixture screw
New float bowl gaskets
New petrol cap o-ring
Reassembled with new throttle cables and a new air filter. Set everything up as standard - needles 2 clicks (46.5-47mm projecting), pilot mixture screw out 1.25 turns, choke as extended as possible (there is still a little bit of movement beyond the closed position on the choke lever I can't seem to adjust out), 2-3mm throttle cable slack, butterfly stop screw set to just touch the butterfly mechanism.
Fired the bike up and it started fine, settled into a tickover and picks up ok. I tinkered with the pilot screw, closing off and backing out and then tweaked the throttle stop screw, all seemed fine and I could get a smooth idle at about 1000 rpm.
Blipping the throttle the engine picks up fine and will rev throughout the range on the centre stand.
I hooked up my ebay vacuum gauge... Tickover seemed balanced, I then managed to burn a hole through one of the tubes on the hot exhaust. The o-ring in the valve on the lhs vacuum gauge doesn't seem to seat properly and after repairing the hole I couldn't get any sensible readings out the thing after a run...
Head out for a run and whilst the bike will rev and isn't particularly lumpy, it is massively down on power. I got it up to an indicated 50mph (probably more like 40mph) at 2k rpm it will pull slowly upward, with larger throttle openings it will accelerate through the rev range without bogging down, but it just won't pull.
To recap. When I picked the bike up a few weeks back, I rode it from Newcastle Upon Tyne to London and it ran fine below 4000rpm.
Following a clean up and some o-ring replacements, it pulled like a train and ran fine over 4000rpm, but badly at lower rpm - I had both pilot jets incorrectly set up (one actually fell out!),
The fact it pulled well before I started to mess things up makes me think this is a fuel thing rather than an electrical thing..
Have I got the needles set incorrectly, is it now running too lean?
Is it possible to mess up the air filter install so it isn't breathing properly?
I've run out of time and we're away for a few days with the kids. I really want to get this running sweetly as Mrs Ade B has a motorcycle camping trip planned when we get back..
A few pics:
Old and new needles
Aux carb assembly, a previous owner had forced a 13mm nut on the spindle mullering the threads. The o-ring was toast and was replaced.
Old and new airfilters
Vacuum gauge with modified tube... (which may get binned) Gauge on the rhs in the pic decided to reset its needle and wouldn't allow me to move it back to the zero point with the screw adjuster, so I reset both just the read the same...
List of parts
