1982 R100RS - Hit Pothole, Backfired and Died
Posted: Mon Oct 26, 2015 10:37 pm
The other day I hit a pothole doing about 15-20mph and my bike sputtered, backfired and died. When I tried starting back up it tried to turn over then backfired again. Nothing. Trying one more time with no result, I flicked the kill switch off and got a pop. Seemed like there was some unused fuel in the cylinders. I checked the fuel on the spot and it's flowing fine. Eventually I ended up having to trailer her back home. Currently, it's not wanting to fire at all.
Before this happened, the bike recently started to stumble around 3500rpms. I assumed this meant I needed to replace old, worn-out jets since I just had a complete tune up. However, now I'm thinking it was the first sign of an imminent ignition issue.
I grounded the plugs to the cylinder head, one at a time, and got spark when I hit the starter. I also get spark when flicking the kill switch off. I should note that initially the sparks were intermittent, though now they seem reliable. I've been doing some tests on ignition components and am getting good voltage and resistance readings. I pulled off the coils and all the resistance readings check out, although I did notice some corrosion inside one of the towers. I cleaned it as best I could and got a good resistance reading when I connected the plug wire. I took off the front cover, cleaned the connections between the ignition trigger unit/hall sensor and the ICU. I checked the kill switch and everything looks clean inside. It seems to function properly when switched from Run to Off. Even though all these tests check out, could I still have faulty coils? Or would a bad Hall sensor still produce spark?
I checked the throttle/choke cables at the carbs and everything is in place. I opened the headlight bucket and everything is securely connected. All lights are functioning properly. I removed the starter cover to check everything there—all looks good. I'm just trying to pinpoint the problem before I blindly spend $500 to replace coils/Hall sensor, etc.
Could the bump have thrown timing or valves off? Has anyone had a similar experience?
Also of note, the bike has a new starter, alternator, diode board, rectifier, plug wires, and plugs. The carbs were recently rebuilt and a proper tune up was completed the day before this happened.
Before this happened, the bike recently started to stumble around 3500rpms. I assumed this meant I needed to replace old, worn-out jets since I just had a complete tune up. However, now I'm thinking it was the first sign of an imminent ignition issue.
I grounded the plugs to the cylinder head, one at a time, and got spark when I hit the starter. I also get spark when flicking the kill switch off. I should note that initially the sparks were intermittent, though now they seem reliable. I've been doing some tests on ignition components and am getting good voltage and resistance readings. I pulled off the coils and all the resistance readings check out, although I did notice some corrosion inside one of the towers. I cleaned it as best I could and got a good resistance reading when I connected the plug wire. I took off the front cover, cleaned the connections between the ignition trigger unit/hall sensor and the ICU. I checked the kill switch and everything looks clean inside. It seems to function properly when switched from Run to Off. Even though all these tests check out, could I still have faulty coils? Or would a bad Hall sensor still produce spark?
I checked the throttle/choke cables at the carbs and everything is in place. I opened the headlight bucket and everything is securely connected. All lights are functioning properly. I removed the starter cover to check everything there—all looks good. I'm just trying to pinpoint the problem before I blindly spend $500 to replace coils/Hall sensor, etc.
Could the bump have thrown timing or valves off? Has anyone had a similar experience?
Also of note, the bike has a new starter, alternator, diode board, rectifier, plug wires, and plugs. The carbs were recently rebuilt and a proper tune up was completed the day before this happened.